April 9 and 13, 2002 meeting notes
In attendance:
John Carmack
Phil Eaton (Tuesday)
Russ Blink
Joseph LaGrave
New Engines
Our stainless steel CNC work from DynaTurn came in, and it
turned out wonderful. I had them make
11 engines, including catalyst chambers, nozzles, spreading plates, and
retaining plates, so we would have enough for two complete vehicles attitude
control, two rotor tip engines, and one test mule. These pieces are combined with Smalley spiral retaining rings as
anti-channel rings, pre-cut stainless screens, copper vacuum flange gaskets,
and pure silver screens that we cut with an arbor punch in our hydraulic
press. We grind down the top of an
aluminum 4 AN fitting for a jet holder, and use Edelbrock stainless steel
flare jets for metering. We finally got
a pressure gauge installed on our hydraulic press, so we now have accurate
measurements of the compression that we do after each anti-channel ring is
installed. For these 1 diameter cat
packs, we go to 500 psi indicated, which, if the external press barrel is fully
loaded, works out to about 1500 psi on the screens.

With a 0.080 jet under an NOS Pro-Race solenoid, these
engines make a very smooth 30 pounds thrust at 600 psi tank pressure, which is
adequate for our attitude control needs in a balanced engine. There is a pretty severe pressure drop
through our packs, which consist of usually 57 20 mesh stainless discs and 70
32 mesh pure silver discs, but we can live with it. Plated screens can get by with less total screens of a coarser
mesh, but we value the fact that we have yet to have a pure silver based pack
wear out at all. I am going to have a
batch of 2 catalyst pack engines machined next week, which can serve as larger
attitude
It has been interesting running the stainless steel engines,
because on a long run, they glow quite visibly red hot. The brass engines get every bit as hot, but
dont visibly glow even on long runs at night.
We fitted four of the new engines, all fully bedded in, to
the big lander, and carried it out for a simple ground test of the attitude
engines. This was also the first test
of our new fill equipment on a vehicle, as opposed to the test stand. We washed the entire system with five
gallons of water, because it had been sitting around for several months
now. We then loaded two gallons of
peroxide, and Russ suited up and set in the seat to run the engines with the
manual push button controller. After
warming (which still involves an initial gush of liquid, unlike the foam
packs), all four engines were initially perfectly smooth, far better than our
previous engines. After a little bit of
running, one of the engines started to have severe pulsing oscillations,
sounding like a machine gun. We had
heard this type of roughness with the foam engines, and we were always
wondering if it was a plumbing issue, or because the engines didnt have jets
in them. We were disappointed to hear
it with the new engines. It is worth
noting that they were still catalyzing perfectly, while the foam engines would
have probably been shot by the end of those runs, which totaled about 60
seconds of firing time on each engine.
To determine if it was related to the plumbing, we switched
two of the engines, leaving the plumbing and solenoid constant. On the second load of two gallons, the same
engine, in its new position, continued to show the roughness. After a little while, a second engine
started behaving the same way, and later a third one started to intermittently
do it.
We are rather confused at the moment. We did note that the first engine to show
the problem was the number 0 engine, which we did a longer set of break in runs
on, so it seems to be a wear or bedding in issue, but we have run similar packs
for many minutes of fire time without showing the problems. There are three differences of note: the packs are now stainless steel, which
will retain somewhat more heat, these runs are at 500+ psi, while all our
recent work has been at 250 psi on the test stand, and these are vertical
firing instead of horizontal.
Next week, we are going to take off the first rough engine
and run it on the test stand at the same feed pressure. That will be an interesting data point one
way or the other, but in all likelihood, we will wind up opening each engine
and adding a couple screens. The higher
heat retention and pressure has probably squashed the silver a little flatter,
so we expect the packs to be a bit loose.
It may just become standard practice to add a few more stainless screens
after running, or perhaps use a higher pack compression during assembly to
deform the silver around the stainless earlier.
We are looking forward to getting the big lander back in the
air. We still have to make a screen
based main engine, but once we do, we should be able to finally get through
long enough series of tests to safely get a person in the air. I also have a significantly changed software
architecture to begin using, and we have the laser altimeter to test.
New Rotor
Our new rotor is assembled.
The list of improvements:
Hub bar made of 7068 aluminum, instead of 6061, for a 2.5x
strength increase
Hub bar inserted and bonded length more than tripled
Better prep for the metal filled epoxy bonding, including a
dilute nitric acid wash
Using 180ksi strength cap screws with proper grip lengths
for retention, three #10 and two ¼ on each hub bar, and two ¼ on each tip
engine mount
Using Kevlar-phenolic board for insulation between the tip
engine and the engine mount
Tip engine mounts made out of 7068 aluminum instead of brass,
for a tip mass savings
Tip engine chambers machined down to save over half their
mass
Tip engine chambers in stainless, for a slight mass saving
and a significant pressure rating increase
Tip engines retained by #10 cap screws instead of #8
Rotor hard line tubing changed to 8000 psi rated stainless
tubing, instead of 2000 psi rated aluminum
The test stand uprights have been rebuilt, with a sturdier
bearing mount.
The blades are set at 20 degrees of pitch, instead of the 10
degrees the old ones were at. There are
concerns about exactly how the rotor retention strength should be calculated
due to multiple attachments and bonding on a long shaft, so we will probably
not spin this much faster than the original, although the higher pitch will
give significantly mote lift. We will
be doing test spins next week, with computer control of the RPM.