April 16 and 20, 2002 Meeting Notes
In attendance:
John Carmack
Phil Eaton
Russ Blink
Neil Milburn
Joseph LaGrave
Motor Jetting
We ran one of the attitude motors (motor label 1) from the
lander on the test stand, and we did still see rough running.
We opened it up, and while the pack did still seemed to
occupy the full volume, it felt a little springier to the touch. I put it back in the press to the same 500
psi indicated (about 1500 psi on the screens) that we originally packed it at,
and it opened up enough area for ten additional stainless screens. Running it again, it was still rough.
We pushed the entire pack out, removed the front spreading
plate, moved a couple of the extra stainless screens to the front of the pack,
and added a spacer under the retaining plate to take up the rest of the
space. It still ran rough, and started
to exhibit the machingun roughness that it had shown on the lander.
We were about to try replacing the bottom three anti-channel
rings, which had gotten a bit loose (although the runs werent cloudy), when we
decided to try a quick jet change from 0.080 to 0.060. The engine got completely smooth again,
although the total thrust had dropped from 32 pounds to 25 pounds.
We then pulled another engine that had been rough on the
lander, ran it on the stand to see if it was still rough, then just changed the
jet without changing anything else. It
was smooth, and only down a couple pounds from the original 32. It looks like the re-compressing of the
first pack closed up enough flow area to drop the extra thrust.
We are leaving the one engine in modified form on the lander
for now.
I finally sat down and worked out the theoretical flow rates
through our jets, which I should have done a long time ago. Many unit conversions ahead, so someone
correct me if I made a mistake:
Our jets are labeled in thousandths of an inch diameter, so
converting to square cm:
2.54*2.54*0.25*3.14159
jet size * jet size * 5.07 = square cm of jet
area
0.060 jet = 0.0182 square cm
0.070 jet = 0.0248 square cm
0.080 jet = 0.0324 square cm
0.090 jet = 0.0411 square cm
Our test stand results are in pounds of thrust, so
converting to peroxide volume flow, assuming a 115 Isp and a 1.4 density:
20 lb/s thrust =
9.09 kg/s thrust =
0.079 kg/s peroxide flow =
0.056 l/s peroxide flow =
56 cm3/s peroxide flow
1000 / 2.2 / 1.4 / 115
pounds thrust * 2.82 = cm3/s flow
20 pounds = 56.4 cm3/s
25 pounds = 70.5 cm3/s
30 pounds = 84.6 cm3/s
35 pounds = 98.7 cm3/s
The fluid velocity through a jet is the volume
flow divided by the jet area. The
Bernoulli equation states that the pressure drop equals the density times
velocity squared divided by two. We
still think in psi, so 1 ps = 1.45e-4 pascals.
1.4e4 kg/m^3 / 2 * 1.45e-4 psi/pa
pressure drop in psi = vel * vel * 1.02
30 pounds with an 0.080 jet = 2.61 m/s = 6.95
psi
30 pounds with an 0.060 jet = 4.65 m/s = 22.1
psi
So, the original jet was only providing a 7 psi
pressure drop, which is not enough to provide much damping at all. When a pack is really perfect, it can run
smooth with no external jet at all, but after a little running, things get
enough out of sorts that we really want to have a reasonable drop to decouple
the combustion chamber from the feed system.
Huzel & Huang recommends a 15% to 20% of chamber pressure drop
across the injector, so even the 22 psi number is probably on the light side
for us, although it isnt exactly clear if the chamber pressure should be
before or after the catalyst pack.
Peristaltic pump
We got a tubing pump to consider for various peroxide
transfer tasks. It pumps 2.8 gpm, and
will push into a pressurized container, so it could be used for loading vehicle
tanks, but there are a couple disadvantages compared to vacuum loading: the
suction isnt nearly as strong (although it self primes just fine), so you have
a harder time getting every last drop out of a small container, and the exit
line will usually hold a bit of liquid.
If we decide to use this for the vehicles, we will have to arrange to
mount the pump at a level above our main control manifold, so all peroxide will
drain down to the manifold, where it will be blown out by the nitrogen
pressurization.
While I was test pumping water into a tank, I did have one
of the hoses blow off the barb and spray water around, so it is worth noting
that hose clamps are mandatory even at under 10 psi pressure
Solenoid water flow tests
The maximum possible peroxide flow through the rotor tip
engines is limited by the amount that can flow through the controlling solenoid
below the shaft, no matter how fast the rotor is spinning. Because a fixed pitch blade takes a certain
amount of thrust to turn a give RPM, if there isnt enough peroxide flow to
generate that thrust, there is no way for it to possibly turn faster than that
if it cant flow enough peroxide through the valve.
We tested the NOS pro-race solenoid at a few tank pressures,
exiting to atmospheric:
100 psi tank pressure = 183 g/s
200 psi tank pressure = 233 g/s
300 psi tank pressure = 283 g/s
If we assume an effective Isp of around 1000 when the
aerodynamic lift is included, that would give us a maximum lift of 512 pounds
at 200 psi tank pressure. With the
previous set of blades, we saw 330 pounds of lift at 645 rpm. The current set of blades has twice the
pitch angle and a little bit longer diameter, so it should produce roughly
twice the lift at a given rpm. Based on
this, it should not be able to spin much over 600 rpm with this solenoid held wide
open.
It should not be possible for us to sling these blades off
with this configuration at rest. If we
replace the solenoid with a ¼ ball valve, we would again have the ability to
overspeed the rotor (and make over 2000 pounds of lift). If we fly at high vertical speeds, the rotor
rpm would also increase.
Rotor RPM control
We have rebuilt the uprights for the vertical test stand,
but I dont have a new 1000 pound load cell yet, so we decided to just do rpm
monitored tests by building a rotor mount on top of our big seated lander. This will allow us to get a vehicle off the
ground very shortly after Space Access.
We will still have to learn how to get the computer to deal with
precession effects, but if we dont wreck it in the process, we should be
flying it fairly soon.
The computer rpm control tests were a big success, with a
few caveats:
We should probably work out some way to get a restricting
jet into the tip engines, because we wind up gushing a fair amount of peroxide
out while warming up. I got more patient
with short pulses and plenty of time to cook off on our later runs.
We had some problems with the RPM sensor on some runs. We will be replacing the trigger bolts with
permanent magnets, which should give a much stronger signal to the sensor for the
next runs.
We heard some popping during the solenoid toggling, which
may well have been vapor phase detonations as new peroxide slammed down the
cavitated lines. It didnt seem to hurt
anything, but it might still be an issue at higher RPM with more mass in the
rotor feed lines. Moving to ball valve
control would probably fix that, and make everything a lot smoother, at the
expense of a more complicated control algorithm.
This is a graph of two separate runs, the first one with a
change from 150 to 175 rpm, and the second one at 200 rpm. The indicated RPM numbers are double actual,
because we had two triggers for the rpm sensor.
media.armadilloaerospace.com/2002_04_20/RotorThrottle.xls
With the rotor on top, our lander now weighs in at a portly
415 pounds, dry. We will be doing our
first precession thruster tests with this vehicle at the 100 acres, but we have
started work on our next generation vehicle, which will finally be designed to
be lightweight. We are aiming to have
it be under 250 pounds, so we can fly it as an ultralight helicopter.