Nov 16 meeting notes

Nov 16 meeting notes:
Location: Long Range Systems
In attendance:
John Carmack
Phil Eaton
Russ Blink
Neil Milburn
Darin Smith
Next week's meeting will be skipped due to thanksgiving. Are we
back to Tuesday after that, or are we moving to Thursday permanently?
I have started the work to get us incorporated so we have some liability
protection.
I have contacted Alpine Insurance (on JP Aerospace's recommendation) about
getting launch insurance for us, since Tripoli experimental launches evidently
won't cover liquid engines.
I wrote a couple differentially throttled flight simulators to get some feel
for how our platform should behave. I was dead wrong about possibly
being able to fly something like this with completely manual controls.
With an attitude sensor and computer hunting to a requested angle, I think we
will be able to do a tethered demonstration flight, but it looks like we are
going to need some axial sensors and more computer control before flying it
completely free.
I spent some time looking into flow regulating valves for our engines.
Relying only on metered jets to control peroxide flow is a significant problem
with catalyst based engines. If some of the peroxide fails to decompose,
the chamber pressure drops, so even more peroxide gets shoved in at a faster
rate, causing less stay time in the catalyst and a vicious circle.
A cavitating venturi is a type of valve that causes a fixed volume of liquid
to flow over a range of pressure deltas. I have been unable to locate
any suppliers on the web, but I did find another type of flow regulating valve
at: http://www.mcmaster.com/catalog/106/html/0348.html
This appears to use sliding plates to vary the flow aperture. The
pressure rating is a bit low, and it has a washer of dubious peroxide
compatibility, but I have ordered a 0.5 gpm flow versions for us to try out.
The fitting sizes are odd, so we will have to adapt on both sides.
If we add chamber pressure sensors, we may just be able to adjust the PWM duty
cycle based on chamber pressure and achieve the same goals, but a mechanical
valve solution would be cheaper and less troublesome.
The PWM driver program now has integrated load cell logging, instead of
forcing me to run a separate program in another window, which will be a big
help next engine test. I need to add an option to let it drive the
latching remote bottle valve as well as the momentary solenoids.
Phil has the solid state relay driver board nicely laid out, with six
channels, integrated LEDs, and connectors for both a parallel port driver or a
micro controller ribbon cable.
Russ machined down a socket to make a catalyst hole punch, which is a big
improvement over cutting the foam with a knife. We compressed the pack
in a press so that we got at least twice as much foam in. We should
count the number of discs, but it is probably difficult to get it apart now.
We should still try and machine a few injector plates with much smaller holes
before we test again. We can test with the old plate and the compressed
catalyst pack first, then change the injector plate if we still aren't getting
good results.
We have 10 liters of 90% peroxide on order from X-L Space Systems. All
future testing should be with peroxide from a common batch, which will remove
a major variable from our results.
We are still waiting on the silver screen order from India.
We are still waiting on the larger load cells from Omega.
We are still waiting on the USB joystick for flight control from the laptop.
We are still waiting on literature for the magnetometers.
We are still waiting on Darin's basic stamps for the accelerometer testing.
We are still waiting on recommendations for leasing a permanent testing site.
We are still waiting on the components for the dumb rocket.
We built the necessary hoses and laid out all the fittings for the VTVL
platform tonight. Russ is going to make a distribution manifold for us
with a quarter in and six eighth outs. We will probably plumb everything
together in parallel with engine development. Even before we have four
working engines for it, we can test all the telemetry and electronics with
just water spraying out of the solenoids.
We have the fill system all loaded onto a cart now, and it is a lot easier to
move around. We still need to secure the catch tank and battery down on
it.
Darin is going to prepare a lecture for us on guidance systems, based on his
time with TI.
The cold weather cracked Russ's peroxide concentrator, so we didn't have any
high test peroxide to fire today. Instead, we did a lot of water flow
tests to characterize the solenoids and plumbing we are using.
20hz pulse frequency, one second total.
100psi 200psi
10% 15ml 15ml
20% 20ml 20ml
30% 27ml 30ml
40% 33ml 39ml
50% 40ml 48ml
60% 46ml 56ml
70% 52ml 67ml
80% 60ml 76ml
90% 68ml 82ml
100% 70ml 95ml
On the 200psi tests, we did notice that we had lost a bit of pressure at the
90% level, and topped it up, so the 70% to 90% numbers are probably a bit
down.
The solenoid did not open at all with a 2ms pulse with 100psi behind it, and a
3ms pulse was not consistent. 2ms pulses works fine without any pressure
behind it, but the pressure obviously effects the responsiveness a lot.
We noted that our water was very cloudy after being ejected from the engine.
Our fill system involves pressurizing with nitrogen after the water/peroxide
is loaded, and it seems to dissolve a fair amount into the water. We
don't know if this is also an issue for peroxide. Yet another reason to
try and find a double ended tank, or plumb a second port in our bottle
manifold for a siphon tube.
We removed the stock bottle manifold and remote bottle valve assembly and
attached the straight shot bottle manifold that Russ had cut. The
not-very-scientific test of blowing through the valves had shown the remote
bottle valve to be much more restrictive than the quarter inch solenoid, and
our successful firing of the large motor seemed to show that it was flow
restricted.
We ran 50% and 100% duty cycle tests, and got the same numbers as before.
This definitively shows that the small 1/8" solenoids we are using are
more restrictive than the remote bottle valve and the manual manifold valve,
so it isn't an issue for us. We will run this test again when we move up
to using the quarter inch solenoids on bigger engines.
We replaced the original manifold assembly, because the pressure gauge and
blow off valve are good measures during testing. However, the straight
out manifold does make for an extremely clean and simple arrangement. It
is tempting to rigidly connect everything together directly onto the bottle
for the dumb rocket, eliminating all flexible plumbing.
We then did a couple tests with the different metering jets we had.
.045" metering jet, 20hz pwm, one second total:
100psi
50% 34ml
100% 56ml
.018" jet
100psi 200psi
50% 14ml 19ml
100% 22ml 30ml
We then put the small engine with the compressed catalyst pack on to see how
much more restrictive the foam bed is now.
Engine with catalyst pack, no jet, 20hz pwm, one second total:
100psi 200psi
50% 38 46
100% 66 94
These are still only minor restrictions in flow. We may still not have
enough back pressure through the catalyst bed.
Our current full throttle engine design targets are roughly 50N thrust for
each engine in the VTVL platform, and 700N for the dumb rocket engine.
If we assume 100s specific impulse, which may be a little conservative, and
1.4g/ml peroxide density, we need to flow 36 ml / second for the small engine,
and 500 ml/second for the large engine.
We don't yet know what our chamber pressures are, so we don't know exactly how
much pressure drop we will have into the engine, but it looks like the
.045" jets are more than large enough for the small engines, and we might
consider some in the .030" range.
Some extrapolation does show that we may have problems with the big engine.
The small solenoids we are using now (super powershot) are rated for 175hp of
nitrous flow, while the largest size available (super big shot) are rated for
600+hp. The remote bottle valve flows noticeably less, so it may only
flow twice as well as the small solenoid, which would probably require
extremely large pressures to get 500 ml/second of flow.
We should test the remote bottle valve without a solenoid at all, but we will
need another solid state relay driver and some minor modifications to the
driver program to control it. We should have the completed driver board
next meeting, so we can do this test before running any peroxide.
We can run 1000psi in our tank if we need to, but we should find out exactly
what combination of pressure, solenoids, and manifolds we need to get the
500ml/second for the big engine. If none of the standard parts can cut
it, Russ wants to make a custom slide valve
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